Mutiny on the HMAS Australia!


A 1919 postcard celebrating the ships return to Australia

When World War One ended, most of the Australian fleet was in European waters. The flagship, HMAS Australia, was released from Royal Navy service and sailed from Portsmouth on April 23, 1919.
The ship stopped in Fremantle, Western Australia on May 28, on the way to her final destination of Sidney. Most sailors anticipated a grand "welcome home" from their grateful nation. Sadly, despite the Allied victory and the outstanding service of the Australians with the Grand Fleet, the return to Australia was a very low key event There were no parades, and no celebrations. Many sailors were somewhat resentful of this, and discontent spread amoung some of the crew.

The visit to Fremantle was the first time that most sailors had seen home in many years, and two days ashore were just not enough time to blow off steam. The Flagship was due to sail from Fremantle on June 1, 1919, and continue to Sidney. Before getting underway, a group of sailors mustered on the quarterdeck, and requested that Captain Cumberlege delay the departure so that the ship's company could have more time to enjoy the 'hospitality' of the local beer halls and female population. After the Captain refused, a number of sailors sabotaged the ship to preventing it from sailing. Lube oil was drained out, valves jammed, and steel wool put into the shaft bearings. The damage was discovered before the machinery was started, so no perminent damage was caused. After an investigation, five seamen were charged with partaking in a mutiny, and were court martialed onboard HMAS Encounter in Sydney Harbour. All were found guilty of 'joining a mutiny without violence', and received prison terms ranging up to two years.

The length of the sentences caused great public outcry. No real damage had been done, the war was over, and the general population felt that the crew was entitled to blow off some steam after serving under the harsh disipline of the Royal Navy. On December 20, 1919, after consulting with the Admiralty and the Government, the sentences were commuted to time served. This outraged officers, and two of the most senior officers in the fleet resigned in protest. Both officers, however, were convinced to withdraw their resignations for the good of the service, and the matter was considered closed. But the incident left a bad taste in the mouths of officers and enlisted men alike, and was not soon forgotten


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